41 complaints reported

1999 Ford F-350 Power Train

Owner-reported problems and safety issues filed with NHTSA. Review common failures, severity levels, and complaint trends over time.

Reports
41
Crashes
0
Fires
0
Injuries
0

Complaint Timeline

Chronological view of owner reports

May 2015

TL* THE CONTACT OWNS A 1999 FORD F-350. WHILE THE VEHICLE WAS AT THE DEALER FOR ROUTINE MAINTENANCE, THE MECHANIC INDICATED THAT THE REAR AXLE WAS FAULTY AND WOULD NEED TO BE REPLACED. ALTHOUGH THE VEHICLE HAD NOT EXPERIENCED ANY FAILURES, THE REAR AXLE WAS REPLACED. THE CONTACT INDICATED THAT APPROXIMATELY 30,000 MILES, LATER THE MECHANIC INDICATED THAT THE REAR AXLE WAS FAULTY AGAIN AND THE AXLE WAS REPLACED A SECOND TIME. AFTER HAVING THE AXLE REPLACED, THE CONTACT WAS UNABLE TO SHIFT TO THE SIXTH GEAR WHILE DRIVING APPROXIMATELY 65 MPH. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 363,000. UPDATED 7/14/15*CN UPDATED 10/16/2017*CN

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: May 2014
Jun 2014

LARGE AMOUNT OF TRANSMISSION FLUID LEAKED OUT ON DRIVEWAY MAKING TRUCK UNABLE TO DRIVE. *TR

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: May 2014
Jul 2004

WHEN ACCELERATING VEHICLE SLIPPED GEAR OR JERKED FORWARD. DEALERSHIP WAS NOTIFIED, BUT DID NOT RESOLVE THE PROBLEM. *AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Aug 2004
Mar 2004

THE VEHICLE'S CLUTCH MECHANISM FAILED WHILE DRIVING. AS A RESULT THE VEHICLE WAS UNABLE TO COME TO AN COMPLETE STOP. PLEASE PROVIDE ANY ADDITIONAL INFORMATION. *NM

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Mar 2004
Mar 2003

THE VEHICLES GEAR SHIFT BROKE OFF THE TRANSMISSION. *NLM

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Mar 2002
Oct 2002

CONSUMER HAS DIFFICULTY GETTING THE TRANSMISSION INTO GEAR AND WHEN SHIFTING, WHEN THE TRANSMISSION DOES SHIFT GEARS, THERE IS A GRINDING NOISE, THE FREE PLAY IN THE CLUTCH IS ALWAYS DIFFERENT, SOMETIMES THE CLUTCH WOULD ENGAGE WHEN THE CLUTCH PEDAL WAS NEAR THE TOP , OTHER TIMES THE CLUTCH WOULD ENGAGE WHEN THE CLUTCH PEDAL WAS PUSHED ALL THE WAY. THE CONSUMER WAS INFORMED THAT THERE WAS A 6 INCH PIECE OF RUBBER HYDRAULIC HOSE IN THE HYDRAULIC LINE OF THE CLUTCH ASSEMBLY, SO WHEN THE VEHICLE WAS WARMED UP, IT EXPANDED INSTEAD OF STAYING RIDGED. FORD IS AWARE OF THE PROBLEM AND UPDATED THE CLUTCH ASSEMBLY, HOWEVER, THE CONSUMER WAS TOLD THAT PROBLEM IS CONSIDERED A WEAR ITEM. *JB *SCC

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Jan 2002
Aug 2002

WE FEEL THIS TRUCK IS A LEMON AND WE WANT SOMEONE TO BE RESPONSIBLE FOR WHAT WE HAVE GONE THROUGH WITH THIS TRUCK, WE HAVE HAD NOTHING BUT TROUBLE WITH IT, IT IS UNRELIABLE.NO SAFETY DEFECT LISTED. *AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Jan 1999
Aug 2002

WHILE CLUTCH IS FULLEY DEPRESSED AND IN GEAR VEHICLE WILL TAKE OFF.CONTACTED DEALER. REPLACED PART, BUT PROBLEM REOCCURRED. *AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Mar 2002
Jul 2002

WHILE DRIVING ON A FLAT SURFACE AT 15MPH, THE VEHICLE LOST ITS CLUTCH. MAKING IT HARD TO STOP THE VEHICLE. DEALER NOTIFIED. *AK THE CONSUMER STATED THAT THE ROLL PIN THAT HOLDS THE HYDRAULIC LINE TO THE SLAVE CYLINDER ON THE CLUTCH HAD COME OUT AND THE LINE DROPPED DOWN. (NO CLUTCH) *SCC

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Jun 2002
Jun 2002

VEHICLE WAS AT A COMPLETE STOP AND MANUAL CLUTCH WENT OUT. VEHICLE LURCHED FORWARD THROUGH A RED LIGHT.*AK.*JB

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Jun 2002
Jun 2002

CLUTCH WAS REPLACED AT 40000 MILES, IT NEEDS TO BE REPLACED AGAIN. MANUFACTURER/DEALER HAVE BEEN NOTIFIED. *AK *SCC

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Jun 2002

PLASTIC SPACER IN CLUTCH ASSEMBLY BROKE, CAUSING CLUTCH TO MALFUNCTION. PLEASE PROVIDE FURTHER INFORMATION.*AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
May 2002

LOW CLUTCH ENGAGEMENT CAUSING THE CLUTCH TO RELEASE WITH PEDAL AGAINST DOWN STOP OR NOT TO RELEASE AT ALL. HAD TRUCK TOWED FOR SAFETY REASONS. WHEN THE CLUTCH DOESN'T RELEASE THIS COULD CAUSE AN ACCIDENT AND FAILURE TO BE ABLE TO STOP VEHICLE WHEN CLUTCH GOES ALL THE WAY TO THE FLOOR AND NOT DISENGAGE CLUTCH. *JG

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: May 2002
Apr 2002

TRANSFER CASE SHIFTING FORK WORE OUT. TRUCK HAD ONLY BEEN IN FOUR WHEEL DRIVE ABOUT A DOZEN TIMES ALL IN SNOW CONDITIONS ON MAJOR HIWAYS. NO OFFROADING AT ALL. HAD TO REPLACE THE SHIFTING FORK, A PLANETARY GEAR AN A IMPUT SHAFT. THIS WAS THE ONLY WAY FORD WOULD SELL THE REPACEMENT PARTS. FORD HAS MADE A DESIGN CHANGE ON THE SHIFTING FORK.*AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Dec 2001
Mar 2002

CONSUMER STATES WHILE DRIVING IN HOT WEATHER THE VEHICLE IS HARD TO SHIFT, THIS PROBLEM ALSO OCCURS OCCASIONALLY WHEN THE WEATER IS NOT HOT, AS A RESULT THE DRIVER HAS TO SHUT THE ENGINE OFF BEFORE AN ACCIDENT OCCURS. NLM

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Feb 2002

VEHICLE WOULD ROLL IN PARKING GEAR. DEALER SAID THAT BEARINGS IN TRANSMISSION WERE WORN COMPLETELY OUT LETTING GEARS BYPASS EACH OTHER. DAMAGE WAS ALSO DONE TO THE TRANSMISSION INTERNAL CASING AND THE GEARS PICTURES ARE AVAILABLE. DEALER PICKED UP 1/2 OF REPAIR COST. HE SAID HE HAD NEVER SEEN THIS PROBLEM BEFORE. DT

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Oct 2002
Sep 2001

WHENEVER DRIVING AT VARIOUS SPEEDS CLUTCH WOULD GO OUT. WOULD HAVE NO PRIOR WARNING. HAD TAKEN TO DEALERSHIP AT LEAST 4 TIMES, AND CLUTCH HAS BEEN CHANGED 4 TIMES. THERE ISN'T ANY INDICATION OF CAUSE OF PROBLEM. IT STILL EXISTS.*AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Aug 2001
Aug 2001

CLUTCH HYDRAULIC RELEASE SYSTEM FAILED CATASTROPHICALLY, CAUSING VEHICLE TO JUMP FORWARD IMMEDIATELY AND VIOLENTLY. FORTUNATELY THE CAR IN FRONT OF ME WAS FAR ENOUGH AWAY SO THAT I DIDN'T HIT IT, BEFORE GETTING VEHICLE STOPPED. ON INVESTIGATION, I FOUND THAT THE ROLL PIN WHICH HOLDS THE CLUTCH LINE INTO THE SLAVE CYLINDER HAD BACKED OUT, AND ALLOWED THE HIGH PRESSURE LINE TO DISCONNECT. WHEN THIS HAPPENED, THE CLUTCH ENGAGED VIOLENTLY, AND THE VEHICLE LURCHED FORWARD ON ENGINE POWER. THIS COULD HAVE CAUSED A MAJOR ACCIDENT, IF ANY OF THE CIRCUMSTANCES HAD BEEN DIFFERENT.*AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Aug 2001
Aug 2001

MANUAL TRANSMISSION CLUTCH ROD CYLINDER BROKE WHILE SHIFTING TO MAKE A TURN. WAS GOING ONLY 25MPH ON A BACK ROAD. WAS ABLE TO RESTART VEHICLE AND DROVE IT HOME. HAD IT TOWED TO DEALERSHIP, AND MECHANIC COULD NOT FIND CAUSE OF BREAKAGE, BUT WAS ABLE TO REPLACE ROD AND SLAVE CYLINDER.*AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Apr 2001
Jun 2001

FOUR WHEEL DRIVE WILL ENGAGE AT ANY SPEED WHILE MAKING A TURN OR STOPPING. DEALERSHIP HAS EXAMINED VEHICLE THREE TIMES, AND CANNOT EFFECTIVELY REMEDY THE PROBLEM. PLEASE PROVIDE ANY ADDITIONAL INFORMATION/ATTACHMENTS. *AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Jan 2001
Apr 2001

PILOT BEARING WENT OUT COMPLETELY, PILOT SHAFT WENT INTO PILOT BEARING. CONSUMER WAS NOT ABLE TO SHIFT GEARS, IT WAS NOT DRIVEABLE. CONSUMER REPLACED PILOT BEARING. CURRENTLY, IT WENT OUT AGAIN. TOOK TO DEALER, AND THEY REPLACED PILOT BEARING AND PILOT SHAFT. *AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Oct 2000
Feb 2001

CLUTCH PEDAL WILL NOT RETURN WHEN APPLIED. VEHICLE TAKEN TO DEALER, AND WAS INFORMED OF A YOKE FAILURE. REPAIRS WERE MADE AT CONSUMER'S COST. DEALER STATED THAT THIS IS NOT AN UNCOMMON PROBLEM. REPLACEMENT PARTS WERE FROM FORD, CONSUMER IS CONCERNED WHY FAILED YOKE IS NOT A MANUFACTURER DEFECT. *AK *TT

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: May 2001
Jan 2001

THE PLASTIC RETAINER LOCATED WHERE THE CLUTCH PEDAL ENGAGES THE ROD FOR THE CLUTCH MASTER CYLINDER WEARS OUT ALLOWING THE ROD TO DISENGAGE THE PEDAL ASSEMBLY WITHOUT ANY NOTICE OF INPENDING FAILURE. THIS HAPPENED TO ME IN A CROWDED PARKING LOT AT THE CANTON TRADE DAYS. LUCKILY I WAS IN 1ST GEAR AND WAS ABLE TO IDLE TO A PARKING SPACE WITHOUT HITTING ANYONE OR ANYTHING. ONCE THE PEDALS COMES LOOSE AND THE ENGINE IS STOPPED IT CANNOT BE RESTARED WITHOUT THE PEDAL ASSEMBLE BEING IN PLACE. THIS PROBLEM CAN BE AVOIDED BY RETURNING BACK TO THE OLD STYLE BALL AND SOCKET SET UP USED ON OLDER VEHICLES AND DOING AWAY WITH THE PLACTIC PIECES IN THE SETUP. HAD I BEEN BEHIND SOMEONE OR BEEN IN A DOWNTOWN DRIVING SITUATION WHERE A PEDESTRIAN BEEN IN FRONT OF ME SUCH AS A STOP LIGHT WHEN IT DECIDED TO COME LOOSE THE OUTCOME MAY HAVE BEEN EXTREMELY SERIOUS. *AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Mar 2000
Dec 2000

WHILE DRIVING ON HIGHWAY TRANSFER CASE BROKE AND VEHICLE WAS NO LONGER ABLE TO RUN. THERE WAS NO PRIOR WARING. CONSUMER HAS CONTACTED DEALER, AND DEALER SAID THEY COULDN'T DO ANYTHING BECAUSE VEHICLE IS NO LONGER UNDER WARRANTY.*AK

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Nov 2000
Oct 2000

WE HAVE EXPERIENCED REPEATED TRANSMISSION PROBLEMS INCLUDING 2 TOTAL BREAKDOWNS, THE LAST ONE ON 09-07-2000 ENDANGERED EVERYONE IN THE VEHICLE. MAY 9, ERATIC SHIFTING, SPEED CONTROL SENSOR HAD TO BE REPLACED, MAY 10 - MAY 22, SHIFTING PROBLEMS CONTINUED, CONTROL MODULE REPLACED. MAY 23, TOTAL TRANSMISSION FAILURE, TRANSMISSION WAS REBUILT ONJUNE 8.. JUNE 29, SHIFTING PROBLEMS STARTED AGAIN. JULY 18, FORD DEALER CHECKED, REPROGRAMED TRANSMISSION AND TOLD ME NO PROBLEMS FOUND. JULY 31, FORD DEALER LOAD TESTED TRUCK, REPLACED MODULE AND REPROGRAMED AGAIN, EVERYTHING OK. SEPTEMBER 7, TOWING TRAILER DOWN 7% - 7 MILE LEWISTON GRADE TRANSMISSION FAILED, LOST ENGINE COMPRESSION BRAKING AND HAD TO RELY ONLY ON BRAKES TO SLOW TRUCK. HAD NO TRANSMISSION IN ANY GEAR WHEN WE REACHED BOTTOM. NEW TRANSMISSION NOW BEING INSTALLED. THIS IS A SAFETY PROBLEM WHICH PLACED EVERYONE IN THE TRUCK IN DANGER.

Type: Vehicle, Vehicle: 1999 FORD F-350, Manufacturer: Ford Motor Company
Incident: Oct 2000

Trend Over Time

Complaints by year

Quick Summary

The 1999 Ford F-350 has 41 Power Train complaints on file. Review the timeline above for detailed owner experiences.